I don't know why ICOM didn't design a lot of their radios to mute the mic when it is keyed from the data port in the back. Its easy enough to overcome this problem if you have a micro-miniature relay.
I bought a couple NEC ud2-5nu 5 volt coil relays. They are VERY small and are double-pole double-throw. This way the PTT button can trigger the relay coil, and there are two available contacts on the relay. The first set replaces the PTT button. The second completes the circuit on the mic element.
This mod is not for the faint of heart. I find that using a diamond-tipped rotary engraver tool to cut the board traces works very well. Once the trace is severed the protective coating can be scratched away leaving enough bare copper to solder some small wires to.
I cut the board traces in three places. One in the hot side of mic line. Second on one side of the PTT button. Third on the other side of the PTT button.
The coil minus side goes right to the common ground plane of the board. This gives the relay something to hold it in place. I put it "dead bug style" on the top of the board, since there is plenty of room in the mic case to mount it. The + side of the coil is fed from the PTT button with the red wire. The other side of the PTT button goes to the +5v supply, with the yellow wire back to the 100uF capacitor.
Relay contacts fed with the black wires replace the PTT button. The other relay contacts bridge the place where I cut the mic trace using the yellow wires at the bottom of the photo.
It may not be pretty, but it works pretty well. The Q1 transistor seems to have enough capacity to supply the hungry relay coil another 20mA of current.
Now I can run my Signal Link for our local NBEMS practice net on FM using my favorite IC-207H radio, and not have to unplug the mic every time the SignalLink keys the radio.
Wednesday, November 13, 2019
ICOM HM-98 mic mod
Monday, October 28, 2019
Amateur Packet Radio
So you may have heard about packet radio in the distant past, but what is it today? Packet radio became a reality in the early 1980's when ASCII (American Standard Code for Information Interchange) was approved as a method for data transmission over the air. It was in its prime until the 90's when the internet took over.
Yes packet radio is the basis for APRS (Automated Packet Reporting System) on 144.39 Mhz, but packet is more than just unconnected packets. Packet can be connected packets finding their way around the world by a hierarchical method of location addressing.
The intricacies of packet are best explained by this series of documents written by WB9LOZ.
Packet is not dead, it is alive today and passing information for the National Traffic System, Bulletin Boards, and personal messages between hams. Packet can get through when the internet can't. Packet is error-free, it may have re-tries but when it does get through, the message crosscheck insures that the data is intact.
Packet operates primarily on RF via the 2 meter band for local hops, and 20 meters for longer hops.
What if you want more? What if your QTH is the only one with access to the BBS backbone of the packet radio network? In that case you may want to become a SYSOP (System Operator). This is the next level of BBS system. It can accept messages and traffic from BBS's via the Internet or from an RF source. It can distribute the internet gathered bulletins and pass messages back through the BBS backbone. In this case you want to look into BQP32. Written by G8BPQ this fully featured software suit will enable your node to become a fully featured BBS net/rom. And there are versions for Linux and Raspberry Pi as well.
If the documentation seems overwhelming, or unclear there is a shortcut for Linux users. Run the bqp-config configuration software from AC0KQ. Run it once, get the settings roughly the way you need, and then don't run it again.
Still confused, need it all step-by-step. NL7OM has the guide for you.
Here is an excellent guide to each parameter in BPQ by AG6QO.
So after all that configuration you are ready to get online. My node is CLYPA:N3FIX on 145.030 Mhz, part of the Underground Packet Network of Central Pennsylvania. This node acts as a digipeater and serves to forward BBS messages and serve the South Central Susquehanna Valley from Cly, PA near 3 mile Island. The antenna is a classic Ringo-Ranger fully restored and mounted on top of the roof fed by LMR-400 coax. The rig is a simple 25 watt Azden PCS-4000 courtesy of KA3LJL. The TNC is a PK-232 MBX running KISS mode operated by a first generation Raspberry Pi running PiLinBPQ software.
Yes packet radio is the basis for APRS (Automated Packet Reporting System) on 144.39 Mhz, but packet is more than just unconnected packets. Packet can be connected packets finding their way around the world by a hierarchical method of location addressing.
The intricacies of packet are best explained by this series of documents written by WB9LOZ.
Packet is not dead, it is alive today and passing information for the National Traffic System, Bulletin Boards, and personal messages between hams. Packet can get through when the internet can't. Packet is error-free, it may have re-tries but when it does get through, the message crosscheck insures that the data is intact.
Look at all the packet activity around the world on the nodemap. There are more than what are shown here.
Packet operates primarily on RF via the 2 meter band for local hops, and 20 meters for longer hops.
- Typical frequencies are on FM 2 meter band: 144.93, 145.01, 145.03, 145.05, 145.07, 145.09 and 145.53 MHz running 1200 baud.
- HF BBS in North America, you can find the "Network 105" BBS on 14.105 MHz LSB running 300 baud.
- There are backbone links between BBS's on 220 and 440 Mhz as well, but most of the local activity for users is on 2 meters.
What if you want more? What if your QTH is the only one with access to the BBS backbone of the packet radio network? In that case you may want to become a SYSOP (System Operator). This is the next level of BBS system. It can accept messages and traffic from BBS's via the Internet or from an RF source. It can distribute the internet gathered bulletins and pass messages back through the BBS backbone. In this case you want to look into BQP32. Written by G8BPQ this fully featured software suit will enable your node to become a fully featured BBS net/rom. And there are versions for Linux and Raspberry Pi as well.
If the documentation seems overwhelming, or unclear there is a shortcut for Linux users. Run the bqp-config configuration software from AC0KQ. Run it once, get the settings roughly the way you need, and then don't run it again.
Still confused, need it all step-by-step. NL7OM has the guide for you.
Here is an excellent guide to each parameter in BPQ by AG6QO.
So after all that configuration you are ready to get online. My node is CLYPA:N3FIX on 145.030 Mhz, part of the Underground Packet Network of Central Pennsylvania. This node acts as a digipeater and serves to forward BBS messages and serve the South Central Susquehanna Valley from Cly, PA near 3 mile Island. The antenna is a classic Ringo-Ranger fully restored and mounted on top of the roof fed by LMR-400 coax. The rig is a simple 25 watt Azden PCS-4000 courtesy of KA3LJL. The TNC is a PK-232 MBX running KISS mode operated by a first generation Raspberry Pi running PiLinBPQ software.
- N3FIX-1 is the BBS server
- N3FIX-2 is the CHAT application
The humble Ringo-Ranger
The humble CLYPA alias node in the basement running unattended.
K3CHB had a good idea to install the Raspberry Pi INSIDE the PK-232. This is a pretty good idea, and I may try that sometime.
Resurrecting a "Watt Weasel"
The Cly Institute has been given the opportunity to resurrect a VHF amplifier based on the February 1971 design in QST magazine by W1SL. Over the years this design has become known as the "Watt Weasel". It employs two 4CX250B tetrode tubes for an achievable output of 1 kw when driven hard with high plate voltage. Since the first 500 watts is what counts, the goal of this restoration is to achieve at least that output linearly. Our benefactor K3WHC has used this amp 30 years back routinely putting out 800 watts.
The original components consist of the PA deck and a Screen / Grid power supply. The original B+ supply has been lost to time and smoke. Therefore, the first big missing piece is to design a new B+ supply with at least 2000 vdc capability. Since our experience at the Institute is with Heathkit SB series HF amplifiers our first thoughts are to employ the technology that we know and trust. An SB-200 runs roughly the same plate voltage and current, therefore a Harbach Electronics PM-200 kit will work nicely here for the B+ supply. It is a voltage doubler circuit that contains all the parts we need to rectify and produce the B+ voltage. The power transformer chosen was an Antek AS-8T800 toroidal-wound transformer. This should give us 800 vac at the high voltage secondary, (with a tertiary winding available for 12 volts or 6 volts if needed.) The transformer can be air-cooled to work into its 1.2 safety factor on voice peaks. Supplying just about half an amp of current will be attainable, and more than we need for our minimum goal.
Here are some photos of the expertly crafted PA deck.
The next task is to insure that the Screen / Grid power supply is operational. This supply as it originally came to us, has a full wave bridge and unregulated Screen voltage which balances out around 310 vdc. In doing some research the Screen voltage around this value may be ok for Class C operation, but not for Class AB1. Some others have insisted that good regulation is needed on the screen supply, whereas this supply has none. The voltage is metered, but the current is not presently hooked up. This Screen current is a good tuning method and should employ the hole in the cabinet for one with a centered needle. A better regulated supply needs to be employed to hold the Screen supply stable with load changes and reduction of secondary emission. That means that the original Screen supply will need to be completely re-worked.
The Grid supply as it arrived to us, is apparently half-wave rectified. It is unregulated and produces about -130 vdc. (Other articles indicate that this voltage should more more around -55 vdc for Class AB operation. There is an adjustment pot for the grid supply, but it only changes a few volts. This seems unsuitable.
To aid in neutralizing the tubes, it will be essential to install a pair of grid current meters to individually monitor grid current. Presently there is no instrumentation on this line. A spare conductor run to the 8-pin Jones-Cinch connector will do well to provide individual grid current measurements. I found some nice edge-reading mA meters for the individual Grid Currents. They will work in the remaining panel real estate.
The final and perhaps the most important issue is the control and interlocking of all the components.
The VHF / UHF DX Book is an excellent publication to refer to on the requirements of feeding the 4CX tube family. The control requirements are like this in order of priority. The availability of the first item on the list permits the second item to start as a permissive. The Grid is negative, so it doesn't matter. Danger exists when the Screen supply is on before the B+. If the Screen starts acting like a Plate, then there will be quick destruction of the tube. If the Grid or B+ fail, the Screen supply must shut down.
1) Air Flow
- Engage Fan and wait for flow switch.
2) Filament Voltage
- (2 minute warmup time)
3) Grid supply
4) B+ supply
- interlocked with relay to Grid supply
5) Screen supply
- interlocked with relay to B+ supply and Grid supply
The more research that was done on regulation of the screen supply lead to a the need for a better screen and grid supply, which would also incorporate a sequence / protection system. Tetrode Boards by GM3SEK offered a ready-made solution with everything that was needed according to my research. The manual is extensive, and requires the boards to be stuffed with the appropriate parts based on the tubes used and design intended. Ian produces a set of printed circuit boards which offer exactly what is needed for tetrode operation and protection. This was the right thing to do. The screen regulator is a shunt type, which can absorb as well as deliver current to the screen. In an unfortunate case of upset and potential flashover, the tube is protected by absorbing energy through the regulator. Zeners are too noisy and cannot absorb the energy. Neons can absorb in the reverse direction but are not precise enough, and cannot guarantee a tight voltage regulation required to eliminate IMD on the tubes caused by variations in screen voltage.
The implication of these boards are that additional voltage is required to allow the regulator to work. The transformers that came with the old supply would not deliver the voltage or current needed. A new transformer was required. Ideally a transformer with a 400 volt winding and two 120 volt windings. An industrial control power transformer is ideal which is why I selected a Hammond 75VA PH75MQMJ. One 120v winding will be used as a primary. The 480v winding is used for the screen supply voltage. To take the stress off the screen / grid regulation circuits, I put an auto-transformer in front of this transformer to dial in the exact voltage required to the Grid / Screen supply.
I may not leave the fan where it is mounted in the photos. It is loud!
The TX and RX relays are both Tohtsu coaxial units. The TX relay has to handle the full power, so its got N connectors. I chose an RX relay as well instead of running separate lines from my XV144 Elecraft transverter. This allows me to run barefoot with the transverter. The limitation of the transverter is that is has no ALC input. So in practice watching the drive level will be critical.
Initial power-up test into a dummy load were good. The amp was able to idle without internal oscillation or unbalance. The neutralization was not disturbed in the PA deck, so it must have been effectively neutralized in the past. The long wait of the warm-up timer before the HV enable relay kicked in was an anxious moment. All the magic smoke stayed in.
The original components consist of the PA deck and a Screen / Grid power supply. The original B+ supply has been lost to time and smoke. Therefore, the first big missing piece is to design a new B+ supply with at least 2000 vdc capability. Since our experience at the Institute is with Heathkit SB series HF amplifiers our first thoughts are to employ the technology that we know and trust. An SB-200 runs roughly the same plate voltage and current, therefore a Harbach Electronics PM-200 kit will work nicely here for the B+ supply. It is a voltage doubler circuit that contains all the parts we need to rectify and produce the B+ voltage. The power transformer chosen was an Antek AS-8T800 toroidal-wound transformer. This should give us 800 vac at the high voltage secondary, (with a tertiary winding available for 12 volts or 6 volts if needed.) The transformer can be air-cooled to work into its 1.2 safety factor on voice peaks. Supplying just about half an amp of current will be attainable, and more than we need for our minimum goal.
The PM-200 Harbach supply uses the standard 0-200uA meter movement in the Heathkit. If we want to monitor both current and voltage simultaneously, all we need is two meters labeled as such. A quick operation on Inkscape after scanning in the original scale, allows us to trace over it and create the appropriate scale which can be printed out 1:1 scale and put on the back of the original scale with contact adhesive.
Easily removed with four screws so we can apply new artwork
The Harbach boards and toroidal transformer work nicely in the 3U rack enclosure box. Cutting out the front panel is the fun part which required a 2" diameter hole and lots of elbow grease.
The power supply layout allows for the low voltage windings to be used for a case circulation fan through the back of the rack enclosure. 5/8" standoffs were used to mount all the boards. As you can imagine the center of gravity WAY to the left side. It produces a healthy 2.1 kilovolts with no load; right on design target.
Modern Technology dictates that a pair of VDR's be installed at each screen to cathode.
Before
Shaft coupler repaired and rotation stops added
After
The next task is to insure that the Screen / Grid power supply is operational. This supply as it originally came to us, has a full wave bridge and unregulated Screen voltage which balances out around 310 vdc. In doing some research the Screen voltage around this value may be ok for Class C operation, but not for Class AB1. Some others have insisted that good regulation is needed on the screen supply, whereas this supply has none. The voltage is metered, but the current is not presently hooked up. This Screen current is a good tuning method and should employ the hole in the cabinet for one with a centered needle. A better regulated supply needs to be employed to hold the Screen supply stable with load changes and reduction of secondary emission. That means that the original Screen supply will need to be completely re-worked.
The Grid supply as it arrived to us, is apparently half-wave rectified. It is unregulated and produces about -130 vdc. (Other articles indicate that this voltage should more more around -55 vdc for Class AB operation. There is an adjustment pot for the grid supply, but it only changes a few volts. This seems unsuitable.
To aid in neutralizing the tubes, it will be essential to install a pair of grid current meters to individually monitor grid current. Presently there is no instrumentation on this line. A spare conductor run to the 8-pin Jones-Cinch connector will do well to provide individual grid current measurements. I found some nice edge-reading mA meters for the individual Grid Currents. They will work in the remaining panel real estate.
The final and perhaps the most important issue is the control and interlocking of all the components.
The VHF / UHF DX Book is an excellent publication to refer to on the requirements of feeding the 4CX tube family. The control requirements are like this in order of priority. The availability of the first item on the list permits the second item to start as a permissive. The Grid is negative, so it doesn't matter. Danger exists when the Screen supply is on before the B+. If the Screen starts acting like a Plate, then there will be quick destruction of the tube. If the Grid or B+ fail, the Screen supply must shut down.
1) Air Flow
- Engage Fan and wait for flow switch.
2) Filament Voltage
- (2 minute warmup time)
3) Grid supply
4) B+ supply
- interlocked with relay to Grid supply
5) Screen supply
- interlocked with relay to B+ supply and Grid supply
The more research that was done on regulation of the screen supply lead to a the need for a better screen and grid supply, which would also incorporate a sequence / protection system. Tetrode Boards by GM3SEK offered a ready-made solution with everything that was needed according to my research. The manual is extensive, and requires the boards to be stuffed with the appropriate parts based on the tubes used and design intended. Ian produces a set of printed circuit boards which offer exactly what is needed for tetrode operation and protection. This was the right thing to do. The screen regulator is a shunt type, which can absorb as well as deliver current to the screen. In an unfortunate case of upset and potential flashover, the tube is protected by absorbing energy through the regulator. Zeners are too noisy and cannot absorb the energy. Neons can absorb in the reverse direction but are not precise enough, and cannot guarantee a tight voltage regulation required to eliminate IMD on the tubes caused by variations in screen voltage.
Rough wiring before the final tye-wrap job.
The implication of these boards are that additional voltage is required to allow the regulator to work. The transformers that came with the old supply would not deliver the voltage or current needed. A new transformer was required. Ideally a transformer with a 400 volt winding and two 120 volt windings. An industrial control power transformer is ideal which is why I selected a Hammond 75VA PH75MQMJ. One 120v winding will be used as a primary. The 480v winding is used for the screen supply voltage. To take the stress off the screen / grid regulation circuits, I put an auto-transformer in front of this transformer to dial in the exact voltage required to the Grid / Screen supply.
Additional markings are needed on the tuning knobs. This will allow a repeat of initial tuning by setting per the dial. These dial markings were made in Inkscape and then printed out and adhered to the plate behind the knob.
The TX and RX relays are both Tohtsu coaxial units. The TX relay has to handle the full power, so its got N connectors. I chose an RX relay as well instead of running separate lines from my XV144 Elecraft transverter. This allows me to run barefoot with the transverter. The limitation of the transverter is that is has no ALC input. So in practice watching the drive level will be critical.
Initial power-up test into a dummy load were good. The amp was able to idle without internal oscillation or unbalance. The neutralization was not disturbed in the PA deck, so it must have been effectively neutralized in the past. The long wait of the warm-up timer before the HV enable relay kicked in was an anxious moment. All the magic smoke stayed in.
The first on air test was done December 18th, 2019 with WA3USG and K3TEF. Other than a little mic hum the signal reports came back clean. The amplifier is operating well within its design limits at 600w out, with no spurious emissions.
The initial relative knob settings are:
Grid Tune = 115
Grid Load = 40
Plate Tune = 134
Plate Load = 13
Kenwood TS-830S - Bandswitches
A customer came to us with this Kenwood TS-830S right out of the 1980's. This hybrid radio isn't something we see everyday. It is clean and well cared for, however the band switch failed to select the 40 meter band with any reliability.
There are lots of notes on how to do this, so I won't go into a lot of detail since someone else has documented this procedure very well. https://www.k4eaa.com/bandswitch.html
Suffice it to say that the band switch contacts were not well attached electrically to the board traces. Many were corroded, or had loose rivets. I saw suggestions on how to attach them with conductive paste. This didn't seem like a good solution, when solder is king! One contact was pretty badly twisted, so that had to be addressed with some fine mechanical adjustment to get it just right.
A fine diamond-tipped engraver was used to clean the corrosion from each contact, rivet, and trace. It was then easy to flux and solder the contacts directly to the board trace. I fixed EACH and EVERY contact in ALL the bandswitches, not just one. They would all eventually all succumb to failure if left alone. Each switch contact slider was treated with De-Oxit and checked for continuity. This fix will outlast the rest of the radio. The plastic parts have already begun to crack.
There are lots of notes on how to do this, so I won't go into a lot of detail since someone else has documented this procedure very well. https://www.k4eaa.com/bandswitch.html
- Pull the final tube nearest the center of the radio, and the driver tube.
- turn the bandswitch to 160m and loosen the setscrew
- turn the bandswitch to 30m and loosen the setscrew
- pull the shaft straight out
- unsolder the 3 wires, and disconnect all connectors
- undo the mounting screw and pull the board out.
Suffice it to say that the band switch contacts were not well attached electrically to the board traces. Many were corroded, or had loose rivets. I saw suggestions on how to attach them with conductive paste. This didn't seem like a good solution, when solder is king! One contact was pretty badly twisted, so that had to be addressed with some fine mechanical adjustment to get it just right.
A fine diamond-tipped engraver was used to clean the corrosion from each contact, rivet, and trace. It was then easy to flux and solder the contacts directly to the board trace. I fixed EACH and EVERY contact in ALL the bandswitches, not just one. They would all eventually all succumb to failure if left alone. Each switch contact slider was treated with De-Oxit and checked for continuity. This fix will outlast the rest of the radio. The plastic parts have already begun to crack.
The RF board wasn't too hard to take out, but there were three wires that had to be unsoldered. One was hidden under the board. (Thanks a lot Kenwood!)
All back together and right on frequency.
Wednesday, July 31, 2019
SB-200 input impedance correction on 10 and 15 meters
I had known that both the 10 and 15 meter band input circuits on my old Heathkit SB-200 linear amplifier were not well matched to my transceiver. Using this amplifier with a newer radio, would cause the transceiver to fold back on these bands with high SWR. Referring to the schematic we see that these employ an L-network to attempt to match the input impedance to standard 50 ohm load.
Going through the mathematical exercise for a PI network, which I won't trouble you with here, it stands to reason this would probably work better just like it does on the lower bands. This more sophisticated matching network filter can have more loss, but that's not something I was worried about. The limited number of turns on the 10 and 15 meter coil meant that they required some fairly small capacitors to attempt to make the matching come out correctly. The problem is that those size capacitors are about the same value of some of the stray capacitance I believed to be in and around the wiring.
The plan was to double the number of turns and increase the capacitance required on the Input side of the network. I then stumbled on this article by PA0FRI who came to the same conclusion.
I stripped the 10 and 15 meter coils from their windings and re-wound with 1mm diameter magnet wire. Scrounging through the junk box yielded the capacitors that I calculated and were confirmed by PA0FRI. I didn't have any tuning caps available, so trial and error yielded appropriate values for the output capacitors which had to factor out the stray capacitance in the wiring.
The trick was how to validate and tune the slugs in the inductors. I've lost the source from a forum post on eHam, but the procedure is to simulate the resistance of the tubes per their data sheet. So we temporarily place a 220 ohm resistor between the filament lead and then to ground on the chassis. While manually pressing in the transmit / receive relay an antenna analyzer is used to measure the impedance at the input connector. After few tweaks of the slugs both bands yielded acceptable impedance at less than 1.5:1 SWR reading.
The final results are below:
Going through the mathematical exercise for a PI network, which I won't trouble you with here, it stands to reason this would probably work better just like it does on the lower bands. This more sophisticated matching network filter can have more loss, but that's not something I was worried about. The limited number of turns on the 10 and 15 meter coil meant that they required some fairly small capacitors to attempt to make the matching come out correctly. The problem is that those size capacitors are about the same value of some of the stray capacitance I believed to be in and around the wiring.
The plan was to double the number of turns and increase the capacitance required on the Input side of the network. I then stumbled on this article by PA0FRI who came to the same conclusion.
I stripped the 10 and 15 meter coils from their windings and re-wound with 1mm diameter magnet wire. Scrounging through the junk box yielded the capacitors that I calculated and were confirmed by PA0FRI. I didn't have any tuning caps available, so trial and error yielded appropriate values for the output capacitors which had to factor out the stray capacitance in the wiring.
The trick was how to validate and tune the slugs in the inductors. I've lost the source from a forum post on eHam, but the procedure is to simulate the resistance of the tubes per their data sheet. So we temporarily place a 220 ohm resistor between the filament lead and then to ground on the chassis. While manually pressing in the transmit / receive relay an antenna analyzer is used to measure the impedance at the input connector. After few tweaks of the slugs both bands yielded acceptable impedance at less than 1.5:1 SWR reading.
The final results are below:
Monday, June 24, 2019
Proficiency in "Radio Sport" helps me at work
For those not familiar with the term “Radio Sport”, it is
the Amateur Radio activity of contacting as many other stations as possible in
a set period of time. This contest
activity involves being able to hear distant stations through noise and
interference, as well as exchanging a precise set of information with the other
station. The exchange of information
must be exact with no mistakes and no misunderstandings. The information is logged for future
reference to be submitted to the sponsoring organization for points. Points are for bragging rights, and the sense
of accomplishment for success. The proficiency
is good practice in the event of supporting communications during an actual
emergency.
In the field of Technical Support, it is important to be brief,
but friendly, and always precise. In the
heat of the moment flowery language is not appropriate, sticking to the subject
with a balance of courtesy is essential.
The skills I learned in Radio Contesting apply well to situations where asking
the right questions without being misunderstood is of primary importance. The client requesting assistance is sometimes
flustered or panicked. Letting them know
you are listening to their problems and calmly providing answers puts the
client’s mind at ease.
Speaking on the telephone with a client while they are in a noisy
equipment room, is not significantly difficult in comparison to a radio conversation
on single sideband with other conversations a few kilohertz up or down the band
bleeding into your own conversation. It
does require a good ear for a person’s voice.
Sometimes during a tech support phone call, the person on the other end
of the conversation may have an accent.
This is commonplace in radio when speaking with radio operators from
around the world. Getting the questions
and answers accurately exchanged when trying to repair equipment using technical
terms can be a challenge. This is where
using the International Phonetic Alphabet to spell things out becomes a great
tool to ensure accuracy. If a part or
model number is confused it could mean sending the wrong replacement to the
client. Misinterpretations resulting in confusion
and delay are not acceptable when a client’s investment is in question. One should not be afraid to ask the person to
repeat themselves or ask them to explain something using different words. Repeating what you have heard is also a good
tool to confirm that the message is received without error or misunderstanding. This practice is commonplace in radio
conversations where noise and interference can often lead to misunderstandings. Being a parrot provides this crosscheck of accurate
information.
In radio conversations the conditions of the band are
usually called to blame for any misunderstandings that may arise, whether that
is the actual cause or not. The person’s
equipment on the other side of the conversation is not called into question, because
that would be confrontational. The same
goes for Technical Support, in that blame is not placed. Avoiding overuse of the word “YOU” keeps the situation
from becoming personal. Always refer to
the problem as a technical task to be overcome, and never succumb to emotional
responses when conversations turn away from objective conversation. My mentor would always say, “They can’t argue
with the science.” If the support
engineer remains objective with an attitude of solving the problem logically,
the person requesting help usually responses with an attitude of gratitude.
When time allows establish a good rapport with the person at
the other end of the conversation. Letting
them know something about you, or listening to something about them, goes a
long way to keeping the conversation friendly.
Listening before speaking goes a long way to let them know they have your
attention and best interests in mind.
As it is done in radio the conversation is ended with a word
of thanks and good wishes. Express your
gratitude for their patience while working through the problem. Apologize when required and stick to the
science.
This is Eric N3FIX.
73
Tuesday, May 28, 2019
Grid Dip Meter
The grid dip meter (or grid dip oscillator) is a useful tool that deserves some interest today. They are often found without their coil sets at hamfests. The grid dip oscillator is instrumented with a current meter on the vacuum tube grid. This indication in the drop in grid current indicates resonance with a nearby tuned circuit. When the resonance of the grid dip oscillator matches with a nearby device the oscillator is loaded as the energy transfers out from the circulating current of the LC tank, and is absorbed by the nearby circuit. The oscillator may be coupled inductively to the coil under test, or capacitively to a coaxial cable. The grid dip meter can also function to find the resonance of an antenna this way.
A secondary function of this particular Heathkit GD-1B grid dip meter is the DIODE mode. This allows a pair of headphones to be inserted into the jack. Tuning the grid dip meter to the resonant frequency of a nearby oscillator will produce a beat tone in the headphones. This can be useful when neutralizing a transmitter.
Other functions naturally include finding the value of unknown inductor or capacitor components against a known capacitor or inductor. Determining the selectivity or "Q" of a circuit is also possible, by observing the sharpness of the grid dip. This function requires the aid of a high impedance volt meter.
Here's the schematic. It draws current from the mains, and has a set of coils. At a swap meet, I was able to obtain a FULL set of coils including the low frequency coils. I knew what they were immediately and snapped them up for a reasonable price. It sure beats trying to re-wind a set of coils yourself. The coil socket is safe due to the capacitors coupling the tank circuit to the vacuum tube terminals, so there is no high voltage DC present to the external connections.
The DC filter capacitors were replaced summarily, and a few of the carbon resistors were replaced as well as they had drifted away from their nominal values. The original dial scale was in decent shape, despite the actual dial being cracked from over-tightening the set screw. It wasn't cracked in half at least. The problem was the that indicated frequency wasn't really that accurate. There was opportunity to make it better.
I removed the scale, and scanned it in. This could then be imported into Inkscape and used as a template to make a new scale. Drawing with Inkscape is a breeze once you get the hang of it. The beauty is that it is all vector drawing, so any line can be re-adjusted with ease. Aspects of the drawing can be separated by layers and even locked or hidden from view. The first step was to create a relative scale, so I put a ring of the alphabet around the dial. This relative scale was used to create a chart of data for making a calibrated dial scale as compared to a frequency counter.
The lower frequencies could be inductively coupled to the frequency counter using a similar coil. The higher frequencies would not couple this way and had to be capacitively coupled into a short coax "antenna" into the frequency counter. Once the table of data was filled in for each coil, then I could finished drawing all the other band scales on the new dial label. Yes, it was tedious, but it was worth it. To get markers on the scales, I added intermediate nodes after the circles were converted to vector paths. This made it easy to sub-divide points between places where I wanted a numeric label. The text was written out in a straight line and then applied to the path. This is a very clever method that I have employed before to get things to look just right. I was able to eliminate the interior relative band scale, and put scales for the two additional low band coils. I made sure 455khz was clearly marked.
A secondary function of this particular Heathkit GD-1B grid dip meter is the DIODE mode. This allows a pair of headphones to be inserted into the jack. Tuning the grid dip meter to the resonant frequency of a nearby oscillator will produce a beat tone in the headphones. This can be useful when neutralizing a transmitter.
Other functions naturally include finding the value of unknown inductor or capacitor components against a known capacitor or inductor. Determining the selectivity or "Q" of a circuit is also possible, by observing the sharpness of the grid dip. This function requires the aid of a high impedance volt meter.
Here's the schematic. It draws current from the mains, and has a set of coils. At a swap meet, I was able to obtain a FULL set of coils including the low frequency coils. I knew what they were immediately and snapped them up for a reasonable price. It sure beats trying to re-wind a set of coils yourself. The coil socket is safe due to the capacitors coupling the tank circuit to the vacuum tube terminals, so there is no high voltage DC present to the external connections.
The DC filter capacitors were replaced summarily, and a few of the carbon resistors were replaced as well as they had drifted away from their nominal values. The original dial scale was in decent shape, despite the actual dial being cracked from over-tightening the set screw. It wasn't cracked in half at least. The problem was the that indicated frequency wasn't really that accurate. There was opportunity to make it better.
I removed the scale, and scanned it in. This could then be imported into Inkscape and used as a template to make a new scale. Drawing with Inkscape is a breeze once you get the hang of it. The beauty is that it is all vector drawing, so any line can be re-adjusted with ease. Aspects of the drawing can be separated by layers and even locked or hidden from view. The first step was to create a relative scale, so I put a ring of the alphabet around the dial. This relative scale was used to create a chart of data for making a calibrated dial scale as compared to a frequency counter.
The lower frequencies could be inductively coupled to the frequency counter using a similar coil. The higher frequencies would not couple this way and had to be capacitively coupled into a short coax "antenna" into the frequency counter. Once the table of data was filled in for each coil, then I could finished drawing all the other band scales on the new dial label. Yes, it was tedious, but it was worth it. To get markers on the scales, I added intermediate nodes after the circles were converted to vector paths. This made it easy to sub-divide points between places where I wanted a numeric label. The text was written out in a straight line and then applied to the path. This is a very clever method that I have employed before to get things to look just right. I was able to eliminate the interior relative band scale, and put scales for the two additional low band coils. I made sure 455khz was clearly marked.
By using the original scan as an image to trace over top, the size and shape was easily determined. The scanned image opacity was reduced to show a ghost image of what I was starting with. You can see the calibration of some of the coils was quite poor, while others were not too far off.
The Cly Institute would like to thank KA3LJL for the donation of this grid dip meter. It will be a good addition to our array of vintage test equipment.
Friday, January 25, 2019
Automatic Radio Mfg. Co. model CL-100
When dealing with transformer-less AM radios a careless touch could be a shocking experience. We've all been warned of the dangers and are not surprised. However, this situation was shocking in another way. When I opened this Automatic Radio Mfg. Co. model CL-100 made in Boston, MA, I discovered that it contained a printed circuit board. According to the information on radiomuseum.org, I was expecting point-to-point wiring. It must be a slightly newer model. I didn't think that printed circuit boards became commonplace till the 60's. I had not encountered an All American Five tube design that incorporated a printed circuit board. According to radiomuseum.org Automatic Radio Mfg. Co. went out of business in 1957. This doesn't sound correct, because I have seen documents of court cases between Ford Mo. Co. and Automatic into the late 1960's.
The backstory on this little clock radio is that it was one that I kept next to by bedside when I was a teenager. I don't think I ever opened it up, I just ran it the way it was with the little bit of hum that it produced. The alarm clock feature provided a soft wake-up as the tubes came alive in the morning when the alarm cam closed its contacts at the appointed hour. The sleep feature provided a way to fall to sleep with music or news and have the radio turn off on its own. It is a pretty clever little device. It came out of the bottom of a box in the basement looking like this. There is a white substance on the knobs, which appeared to be mold?!?! (I have noticed this on the old Magnavox TV that is still in that basement.)
The case opens easily by popping the cardboard back off. That will need some tender loving restoration as it has begun to split. The tag is still legible, but doesn't really contain a year of manufacture. The quality control stamps are still visible. I only gently cleaned the chassis because it has a nice protective layer of waxy cosmoline on it. This protective layer has preserved the chassis and all the components from any oxidation. I've seen this on a few circuit boards in the past, but not as generous an application on a tabletop radio like this.
The knobs pop off and the four screws in the bottom allow the chassis to slide out. The only trick was gently prying off the clear front pieces so that the tuning pointer could be removed. The once bright and shiny gold bezels are faded. I think that some gold leaf paper from the craft store would look grand when properly cut and pasted in. There's no preserving what is there. It looks awful.
The plastic case itself is unbroken, but scratched and marked. Some gentle rubbing with a Mr. Clean magic eraser pad cleared off the marks. Some additional polishing to buff out the case may be needed as final preparation for re-assembly. Overall it looks good for its age, and only one knob is missing.
The cosmoline impregnated a lot of dust on the top of the board over the years and I decided to leave it alone. It ran when parked, remember. All it should need is a few capacitors and maybe an alignment tweak. The capacitors were all common values and quickly replaced. The circuit board itself is strong, but the traces are pretty fragile. Much care was given to keep from destroying the integrity. The main filter cap was easily pulled out with only minor damage to the surrounding traces. A dremel tool easily sliced through the electrolytic body after removing the cardboard cover. Once free the base of the original capacitor is re-usable as a carrier for the new filter capacitors. They are too big to fit in cross-ways, but fit nicely stacked one on top of the other with some lead extensions. The mounting leads had to be drilled through to make contact with the actual contacts since the interior of the rivets and feed wires out of the original capacitor guts are aluminum. The cardboard cover was re-used to hide the capacitor modification.
What is this big mystery component in the middle of the board? It is large and square. Is it a resistor / capacitor network? I didn't pay much attention as long as the radio decides to play.
Which it did after all the paper capacitors and burst bumble-bee cap was replaced. And it plays beautifully with no hum and good station selectivity. To make it safe a new cord is in order.
Directing our attention back to the case, the bezels needed attention to make this piece of atomic age art presentable. I visited the local craft store and found some nice bronze-colored plastic film. It is quite thick and actually challenging to cut with a razor blade. I think it will work just fine hidden behind the plastic bezels.
For a final product, I would say that it turned out really well. It looks the part, it plays, and it keeps time. What more could I want !
The backstory on this little clock radio is that it was one that I kept next to by bedside when I was a teenager. I don't think I ever opened it up, I just ran it the way it was with the little bit of hum that it produced. The alarm clock feature provided a soft wake-up as the tubes came alive in the morning when the alarm cam closed its contacts at the appointed hour. The sleep feature provided a way to fall to sleep with music or news and have the radio turn off on its own. It is a pretty clever little device. It came out of the bottom of a box in the basement looking like this. There is a white substance on the knobs, which appeared to be mold?!?! (I have noticed this on the old Magnavox TV that is still in that basement.)
The case opens easily by popping the cardboard back off. That will need some tender loving restoration as it has begun to split. The tag is still legible, but doesn't really contain a year of manufacture. The quality control stamps are still visible. I only gently cleaned the chassis because it has a nice protective layer of waxy cosmoline on it. This protective layer has preserved the chassis and all the components from any oxidation. I've seen this on a few circuit boards in the past, but not as generous an application on a tabletop radio like this.
The knobs pop off and the four screws in the bottom allow the chassis to slide out. The only trick was gently prying off the clear front pieces so that the tuning pointer could be removed. The once bright and shiny gold bezels are faded. I think that some gold leaf paper from the craft store would look grand when properly cut and pasted in. There's no preserving what is there. It looks awful.
The plastic case itself is unbroken, but scratched and marked. Some gentle rubbing with a Mr. Clean magic eraser pad cleared off the marks. Some additional polishing to buff out the case may be needed as final preparation for re-assembly. Overall it looks good for its age, and only one knob is missing.
The cosmoline impregnated a lot of dust on the top of the board over the years and I decided to leave it alone. It ran when parked, remember. All it should need is a few capacitors and maybe an alignment tweak. The capacitors were all common values and quickly replaced. The circuit board itself is strong, but the traces are pretty fragile. Much care was given to keep from destroying the integrity. The main filter cap was easily pulled out with only minor damage to the surrounding traces. A dremel tool easily sliced through the electrolytic body after removing the cardboard cover. Once free the base of the original capacitor is re-usable as a carrier for the new filter capacitors. They are too big to fit in cross-ways, but fit nicely stacked one on top of the other with some lead extensions. The mounting leads had to be drilled through to make contact with the actual contacts since the interior of the rivets and feed wires out of the original capacitor guts are aluminum. The cardboard cover was re-used to hide the capacitor modification.
What is this big mystery component in the middle of the board? It is large and square. Is it a resistor / capacitor network? I didn't pay much attention as long as the radio decides to play.
Which it did after all the paper capacitors and burst bumble-bee cap was replaced. And it plays beautifully with no hum and good station selectivity. To make it safe a new cord is in order.
Directing our attention back to the case, the bezels needed attention to make this piece of atomic age art presentable. I visited the local craft store and found some nice bronze-colored plastic film. It is quite thick and actually challenging to cut with a razor blade. I think it will work just fine hidden behind the plastic bezels.
For a final product, I would say that it turned out really well. It looks the part, it plays, and it keeps time. What more could I want !
Wednesday, January 9, 2019
Silicone Grease
Silicone is a wondrous material. It has so many uses and comes in quite a few forms.
Let us consider Silicone Grease. It exhibits excellent dielectric properties. It can be used inside UHF connectors before they are wrapped for outdoor waterproofing. It can be used on spark plug wire boots to facilitate easy removal. Silicone grease is safe for plastic and paint. It can be applied as a lubricant to plastic, such as drawer runners. Lubricating refrigerator drawers is my XYL's favorite usage.
I have used it to lubricate sticky mic PTT buttons. (No one wants to be THAT guy who gets his mic stuck on keying the repeater for hours.)
de N3FIX
Let us consider Silicone Grease. It exhibits excellent dielectric properties. It can be used inside UHF connectors before they are wrapped for outdoor waterproofing. It can be used on spark plug wire boots to facilitate easy removal. Silicone grease is safe for plastic and paint. It can be applied as a lubricant to plastic, such as drawer runners. Lubricating refrigerator drawers is my XYL's favorite usage.
I have used it to lubricate sticky mic PTT buttons. (No one wants to be THAT guy who gets his mic stuck on keying the repeater for hours.)
de N3FIX
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